Midnight Special
Well-known member
...Having experienced boil-over issues with TJ's (low mile) 289 and replacing numerous stats, caps, shroud, flushing radiators and reading over & over the posts here by Arlie, Marty & like on the subject, TJ came to me Friday evening and said "Dad, we're going after those head gaskets!". (Rob - I swear he's YOUR kid! ;-)
Something has been pressurizing the cooling system and forcing the water out over time since the new motor was installed. It didn't get hot unless levels were low and there was no steaming exhaust or power loss, but something wasn't right. He's always had to add water about every four days of daily driving. With all other means tried - we figured why not.
So into it he goes! We pulled the intake and heads, cleaned, inspected, checked for warpage, cracks and vallah! a small breach (separation) in the gasket that looked to be tossing compression into a water channel!
I am posting this to hopefully end any further head scratching and to give validity to to an otherwise unpleasant task. Total time for us amateurs was about 8 hours...
Upon replacing the head & intake gaskets, the results were magnificent! No water loss, smoother idle and no boil-over during about two hours of test driving.
Something has been pressurizing the cooling system and forcing the water out over time since the new motor was installed. It didn't get hot unless levels were low and there was no steaming exhaust or power loss, but something wasn't right. He's always had to add water about every four days of daily driving. With all other means tried - we figured why not.
So into it he goes! We pulled the intake and heads, cleaned, inspected, checked for warpage, cracks and vallah! a small breach (separation) in the gasket that looked to be tossing compression into a water channel!
I am posting this to hopefully end any further head scratching and to give validity to to an otherwise unpleasant task. Total time for us amateurs was about 8 hours...
Upon replacing the head & intake gaskets, the results were magnificent! No water loss, smoother idle and no boil-over during about two hours of test driving.